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Old 12-19-2015, 09:57 AM   #1
sevndaythry   sevndaythry is offline
 
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Head Scratching Hawk 250 decided to retune itself?

So about a week and a half ago I ran out of fuel earlier than expected (guess I'm getting more comfortable on it), and had to switch to the reserve. I went straight to a gas station and filled her up and didn't think anything of it. seemed to run normal the rest of my ride to work (had spots of weak power like it was running a bit lean). on the way home later that day the weak power spots seemed to be worse, so I took the stock carb off and sprayed it down with carb cleaner I never removed the bowl(didn't want to drill it). It was late so I didn't test ride it.

The next day we were heading out for a ride and it started driving like absolute garbage. seemed to be able to throttle through it, but don't have any useable mid range, super low or WOT. We hit some trails and did some wheelie practice other that limited throttle range the bike rand "fine".

The next day we had plans to pull the carb and drill the bowl off. Did that, cleaned the carb, had problems with the gasket swelling (anyone know how prevent this?) ended up having to remove some of the O-ring bowl gasket to shorten it.

To make a week long story shorter:

After putting it back together and many disassembly/reassembly iterations later I have diagnosed that my needle jet has grown in size all by itself.

The bike Idles fine. From 1/4-5/8 the bike is rich as all get out. 5/8 and up feels fine(might be a little lean, or only make 14hp).

I have made many adjustments to the pilot screw and none seem to have any effect.

Im almost positive my problem lies in the transition from pilot circuit to main circuit. But what would cause an unmodified bike to suddenly change like that?

I have a rebuild kit for the keihin clone on the way, and a mikuni clone coming as well. Its a race to see what gets here first. This has been so frustrating, and the worst part is I can't even go for a ride to relax



Problem Update:
Check your air Filter for restrictions. Mine was soaked in oil starving the engine of adequate airflow.



Last edited by sevndaythry; 01-10-2016 at 09:55 AM. Reason: added solution to end of problem.
 
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Old 12-19-2015, 01:49 PM   #2
2LZ   2LZ is offline
 
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Sounds to me like the pilot jet is still clogged. I'd take it back apart and reclean.
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Old 12-20-2015, 02:49 PM   #3
Adjuster   Adjuster is offline
 
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You had to shorten the bowl gasket? I believe the bowl has to be completely air tight. Did shortening the gasket cause a possible air leak.


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Old 12-20-2015, 02:53 PM   #4
Adjuster   Adjuster is offline
 
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By the way its interesting you mentioned the bike retuned itself. The same thing happened to me. My idle speed dropped way low and the fuel mixture appeared to be way off. I think maybe its because we had a weather cold front come through. Went from mid 80s and extreme humidity to 0 humidity and mid 70s. Could a weather low pressure front cause this?



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Last edited by Adjuster; 12-20-2015 at 04:11 PM.
 
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Old 12-20-2015, 09:45 PM   #5
Panic-Pete   Panic-Pete is offline
 
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A word to swollen, gasoline or solvent-soaked gaskets and o-rings.
These shrink back into their proper size, after airing and drying thoroughly.
The same goes for diaphragms, for example, in cv-carburators. (That good quality parts shouldn´t swell and soak at all or that much... is a different matter...)

Carburator bowls don´t have to be airtight. In fact they have vents...though these days, they´re led into some emission control systems.

Of course, the bowl should be liquid-tight.

I go along with the thesis of a clogged idle (primary) jet. (..but the needle valve may be cleaned, adjusted and tested as well.)


regards

Panic-Pete
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Old 12-21-2015, 12:46 AM   #6
Jay In Milpitas   Jay In Milpitas is offline
 
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Slide or diaphragm carb?

I'm not at all familiar with your bike, so only speculating here.

When you took the carb apart, is there a chance the slide got installed backwards (turned around)?

Is it possible the needle got dislodged and pushed up higher in to the slide?

Every thing that Pete says holds true, too.


 
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Old 12-22-2015, 10:25 PM   #7
sevndaythry   sevndaythry is offline
 
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Sorry for the late response. So I've gotten a rebuild kit for the stock carb, that has an adjustable needle. I also received my mikuni clone. Both carbs have the same effect. The mikuni came with a 20slow and 100 main. Whenever I do a plug chop the plug is black as all get out. Everything is where it's supposed to be. I'm soooo confused. Earlier this evening I was futzing with it and it idled best on full choke, and would eventually die after I opened it up. Anything after idle, choppy sputtering and backfiring. Could it be ignition related? Arrrrrgh


 
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Old 12-22-2015, 10:54 PM   #8
sevndaythry   sevndaythry is offline
 
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As for shortening the gasket, i let it sit overnight and even tried putting it in the freezer there was just too much material. I took the material out of the straight sections on the side and it holds fuel just fine.


 
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Old 12-23-2015, 10:46 AM   #9
Weldangrind   Weldangrind is offline
 
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The stock Mikuni jetting is way too lean, unless you're at 10000 feet.
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Old 12-23-2015, 01:30 PM   #10
sevndaythry   sevndaythry is offline
 
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My concern and what is so confusing, is at any amount of throttle when it gets all choppy the plug is black and sooty as can be.


 
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Old 12-23-2015, 02:39 PM   #11
2LZ   2LZ is offline
 
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Quote:
Originally Posted by sevndaythry View Post
My concern and what is so confusing, is at any amount of throttle when it gets all choppy the plug is black and sooty as can be.
Black and sooty? The stock jetting should be showing lean....REALLY lean. Like Weld says, 10,000 feet lean. Did you by chance knock the float setting when the bowl was off? They're very delicate and can be tweaked easily. Black and sooty usually means dumping fuel.
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Old 12-23-2015, 04:19 PM   #12
sevndaythry   sevndaythry is offline
 
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I know. Float level is in spec. This is why I'm so confused. Nothing is making sense.


 
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Old 12-24-2015, 01:07 AM   #13
Weldangrind   Weldangrind is offline
 
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What RPM was the plug chop performed at (roughly)? Idle, part throttle or WOT?
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Old 12-24-2015, 07:41 AM   #14
sevndaythry   sevndaythry is offline
 
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The engine usually starts breaking up 1/8---1/2 throttle. I've done a few of them, the most recent were at about 1/4.


 
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Old 12-24-2015, 11:00 AM   #15
Weldangrind   Weldangrind is offline
 
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That could strictly be clip position. Clean the plug, and try a plug chop at idle.
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